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Grönwall, Fred, 2010. Optimization of Burner Kiln 7, Cementa Slite. Second cycle, A2E. Uppsala: SLU, Dept. of Energy and Technology

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Abstract

In this report focus is put on the combustion process at a cement plant. Combustion is the
heart of the cement making process and absolutely crucial to have under full control and well
optimized.

The fuel is put into the process through a burner pipe and this burner pipe is modified to
reach a more efficient combustion. The primary target is to enable burning of heterogeneous
alternative fuels and increase the production level. Other positive effects from this type of
optimization is lowered specific fuel consumption and lowered CO2 emissions.
A redundant burner is chosen for the project and overall the project steps are the following:

1. Installing a Jet air nozzle ring in a way so it can move both axially and radially due to
temperature changes.

2. Remove the present refractory from the burner and order a new form to decrease the
weight of the burner

3. Place a K6 blower in operating the axial channel.

4. Install Gauging equipment (Temp, pressure, ampere blower etc)

5. Carefully observe process values during the modified burners run in time.

6. Evaluate the results of the project

7. With the help of proven potential in the kiln system be able to convince management
of the proceeds to invest in a new burner

8. If point 7 is fulfilled with the help of experience, be able to operate as a project
coordinator in the purchase of a professional burner. This task will include
coordinating the project group in various meetings and then lead to an RFQ (Request
For Quotation).

Results from the project show the great potential in an optimization of a burner at a cement
plant. A production increase of 5% could be seen together with a lowered specific energy
consumption which is extremely satisfactory results. Unfortunately a breakdown of the
system occurred a bit down the path of optimisation that resulted in damages to the kiln. At
this stage the optimization was stopped and the old burner was put back after finished kiln
repair.

Finally crucial to underline is that the proven results in this study convinced the Group
Management of buying a new burner. The benefits from a professional tailor made burner are
far greater than the cost of buying it. The payback time is roughly around a year for such an
investment depending on current market conditions.

Main title:Optimization of Burner Kiln 7, Cementa Slite
Authors:Grönwall, Fred
Supervisor:Larsson, Johan
Examiner:Johansson, Tord
Series:Examensarbete / Institutionen för energi och teknik, SLU
Volume/Sequential designation:2010:07
Year of Publication:2010
Level and depth descriptor:Second cycle, A2E
Student's programme affiliation:TENSY Energy Systems Engineering (admitted before July 1, 2007) 270 HEC
Supervising department:(NL, NJ) > Dept. of Energy and Technology
Keywords:cement, combustion, energy, fluid Mechanics, process Industry
URN:NBN:urn:nbn:se:slu:epsilon-8-917
Permanent URL:
http://urn.kb.se/resolve?urn=urn:nbn:se:slu:epsilon-8-917
Subject. Use of subject categories until 2023-04-30.:Energy resources management
Chemistry
Technology
Language:English
Additional Information:Relaterad länk (Uppsala universitets publiceringsdatabas DIVA): http://urn.kb.se/resolve?urn=urn:nbn:se:uu:diva-148689
Deposited On:21 Dec 2010 09:31
Metadata Last Modified:15 Jan 2014 15:41

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